Surface milling and grinding are widely used in the fabrication of free-form surfaces
for molds and dies. The continuous demand for better product quality has led to
demand in higher surface accuracy. Limiting factors are the positioning accuracy of
the tool and the accuracy of the manufacturing process. Computer controlled
surfacing (CCS) has been developed mainly for the fabrication of aspherical and
freeform surfaces. The surface is repeatedly measured and corrected using abrasives
until the target accuracy is attained. In principle, sub-micron accuracy is achievable.
The accuracy is limited by surface measurement and not by the processing
equipment.
The current research investigates the adoption of CCP for the fabrication of freeform
surfaces for molds and dies. The test-bed is based on a 6-axis RX robot as the
motion platform with a spindle attached to the wrist of the robot. The positioning
accuracy of the robot is estimated to be no better than 0.05- 0.1mm. Surface
measurement is carried out using a Talysurf PGI surface profiler. Surface error
correction is performed by removal of material from the surface through abrasion.
The amount of material to be removed in each iteration is based on the measured
surface error.
Various material removal processes have been evaluated for surface correction.
They involve using either bond abrasives or loose abrasives. A number of tool
design options were investigated. Experiments were performed to evaluate the
processes in terms of the material removal rate, process stability, etc.
The current work on surface correction assumes a predetermined tool path. The feed
rate along the tool path for surface correction is to be varied locally according to the
required amount of material to be removed. Three algorithms were adopted /
developed for the feed rate calculation. They are table look-up, discrete convolution
and influence function offsetting method. Performance of these algorithms was
evaluated through simulations.
A free-form surface specimen of aluminium of about 25mm by 25mm across was
used for the initial experiments. The surface was prepared by CNC surface
machining before polishing. Through repeated measurement and surface correction,
the peak to valley error of the surface was improved from 20 micron to 4.2 microns
within a 20mm by 20mm surface region, and the surface roughness was improved
from 496 nanometer to 13 nanometer.
| Date of Award | 2 Oct 2008 |
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| Original language | English |
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| Awarding Institution | - City University of Hong Kong
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| Supervisor | Hon Yuen TAM (Supervisor) |
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- Surfaces (Technology)
- Iterative methods (Mathematics)
Improvement of surface form accuracy through iterative corrections
YIU, K. L. (Author). 2 Oct 2008
Student thesis: Master's Thesis